I just finished assembling my farmbot, I’m now trying to calibrate movements and endpoints.
My Y-axis motor acts funny, it stutters (see video) during acceleration phase. Then, after the first few seconds of acceleration, it works regularly.
But this leads to “failed movement”.
To remove any possible friction I just isolated the engine from the belt as you can see on the video.
Any help is very appreciated. Please consider I’m very new to farmbot.